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- Subject: AUSROC II: A Post Mortem
- Message-ID: <19519.2b2f721a@levels.unisa.edu.au>
- From: etssp@levels.unisa.edu.au
- Date: 16 Dec 92 18:14:50 +1030
- Reply-To: steven@sal.levels.unisa.edu.au
- Distribution: world
- Organization: University of South Australia
- Lines: 617
-
- This paper was presented by Tzu-Pei Chen at the 1992 AUSROC conference,
- Adelaide, Australia, December 1992.
-
-
- AUSROC II : A Post Mortem
- ~~~~~~~~~~~~~~~~~~~~~~~~~
- Tzu-Pei Chen
-
-
-
-
- Abstract - The AUSROC II Amateur Rocket malfunctioned at
- launch. The LOX valve failed to open fully, preventing the
- rocket from lifting off. Pneumatic and electrical umbilicals
- burnt through preventing an abort sequence. An internal fire
- started in the lower valve fairing and spread throughout the
- rocket, eventually destroyed the payload. A design fault in
- the pressurisation mechanism allowed oxygen to enter the
- kerosene tank resulting in an explosion which destroyed the
- vehicle. No definite reason for the LOX valve failure has
- been found, but a seal failure in the LOX valve vane
- actuator seems the most likely cause. Simple changes to both
- the rocket and launcher systems could have prevented further
- damage to the vehicle after the LOX valve failure. A second
- vehicle designated AUSROC II-2 will be built incorporating
- these changes. This paper describes what is known about the
- launch event. It proposes possible reasons for the failures
- which were encountered, and suggests solutions where
- possible.
-
-
-
- I. INTRODUCTION
- ~~~~~~~~~~~~~~~~
- "If one part fails the whole thing can fail. It's
- not like a car, if you get a flat tire, you stop
- and put another one on ... if you blow a valve,
- you'll probably blow up your tanks and everything
- along with it."
- Mark Blair, March '92
-
- On October 22nd 1992 at about 10:15am an attempt was made to
- launch the AUSROC II Amateur Rocket at the Woomera
- Instrumented Range. A series of malfunctions occurred which
- resulted in a failure to launch, and subsequently led to an
- explosion and total destruction of the vehicle.
-
- At 7:00am the 3 hour Flight Firing Sequence commenced. The
- helium pressure bottle was pressurised to 20MPa and the
- launcher elevated. The kerosene tank was then filled. A dry
- nitrogen supply was connected to the LOX tank and the LOX
- valve opened. The LOX system was then purged for 5 minutes
- to remove any moisture from the LOX feed system especially
- the LOX ball valve. The lower valve fairing was inspected
- visually for any signs of kerosene leakage, and then sealed.
- At T-30'00", LOX fuelling commenced, and was completed 8
- minutes later. It was observed that only a light frost
- formed on the tank walls when full. At this point kerosene
- was discovered to be dripping from the base of the rocket.
- The amount of leakage was assessed to be insignificant, and
- a decision to continue with the launch was made.
-
- At T-15'00" the Final Arm & Launch Sequence began. The
- ignition circuit was connected and all personnel were
- cleared from the launcher. At T-2'00" the automatic launch
- sequence was initiated. Forty seconds later at T-1'20" an
- ABORT was called. The picture from the onboard camera had
- suddenly deteriorated. The countdown was held while the
- problem was discussed, 10 minutes later the automatic launch
- sequence was restarted at the T-2'00" mark.
-
- At T-5s, the electric match fired, and the ignition flare
- ignited successfully. At T-3s the helium valve opened
- pressurising both propellant tanks. At T-0.25s the kerosene
- valve opened (as the kerosene takes about 250ms to travel
- through the regenerative cooling passage of the motor). At
- T=0s the LOX valve was actuated, but failed to open fully,
- resulting in insufficient thrust to lift the vehicle. An
- attempt to abort the launch was made at T+2s, but the
- massive kerosene plume had burnt through nearby ground
- pneumatic lines preventing the abort system from closing the
- propellant valves. At the same time a crackling or popping
- sound could be heard. Eventually, at around T+10s, the more
- characteristic "thrusting" sound developed and the plume
- became much brighter indicating that some oxygen was present
- in the chamber. Kerosene continued to be expelled under
- pressure until T+15s. At around T+20s the electronics
- umbilical was also destroyed preventing switch off of the
- payload. With the payload control lines cut, the payload's
- timer, thinking the rocket had left the launcher, started a
- 55s countdown to deploy the recovery mechanism.
-
- A small fire could be seen at the bottom of the motor, the
- remaining kerosene dribbling from the rocket burning
- brightly in oxygen. Kerosene on the ground and around the
- launcher also continued to burn with a much redder flame.
- >From the onboard camera, smoke could now be seen streaming
- from the upper valve fairing. At T+1'16" the payload fired
- the nose separation pins, and then the nose push rod, 2
- seconds later. The nose cone popped off to one side, and
- fell to the ground. At T+1'25" the payload failed, and all
- telemetry except for the video was lost. At T+1'40" the
- video transmitter stopped.
-
- The flame at the bottom of the motor continued to burn
- brightly. The fire around the launcher eventually went out
- about 1 minute later. At T+3'45" a mixture of kerosene and
- oxygen exploded in the kerosene tank, rupturing the tanks
- cable duct. The expanding gases tore out both the lower
- valve, and intertank fairing hatches, and then sheared the
- bolts fixing the intertank fairing to the LOX tank. The LOX
- feed line was severed at the LOX tank boss, and the rocket
- was blown in half. The remaining LOX pressure was sufficient
- to lift the top half of the rocket off the launcher rail,
- and propel it through the air and then along the ground for
- some tens of metres.
-
- After a 30 minute cool-off time and careful examination of
- the wreckage from the periscope in EC2, the operations
- manager and range safety officer proceeded to the launcher
- area to make the area safe. Mains power was removed from the
- area, and the pyrotechnic cutters associated with the main
- parachute were disarmed. The various pieces of wreckage were
- gathered together and brought back to Test Shop 1 for
- examination.
-
- The upper portion of the rocket was severely dented, and
- disassembly was not possible on the day. Most of the
- fittings in the lower valve and intertank fairings were
- either missing or very badly burnt. The engine however was
- removable and it was discovered that the LOX valve had
- indeed opened by about 10 degrees.
-
- The immediate conclusion, reported by most of the media on
- the day, was that the LOX valve had frozen shut, possibly
- due to the extended countdown. Eventually it was decided
- that this was unlikely considering the low humidity on the
- day and the fact that the dry nitrogen purge should have
- left nothing to freeze within the LOX valve. The preferred
- explanation was that one of the pneumatic lines, probably
- already burning due to the kerosene leak, had burnt through,
- just as the LOX valve was opening [1].
-
- The remains of the rocket were shipped back to Salisbury to
- be fully dismantled. The motor, and the remains of plumbing
- from the lower valve fairing were brought back to Melbourne
- for inspection.
-
-
- II. FAILURE ANALYSIS
- ~~~~~~~~~~~~~~~~~~~~~
- "The price one pays for pursuing any profession,
- or calling, is an intimate knowledge of its ugly
- side."
- James Baldwin
-
- As described above, there were in fact several malfunctions,
- some of these prevented the launch of the rocket, some
- contributed to the subsequent destruction of the rocket, and
- some were simply embarrassing. The major failures which will
- be discussed are;
-
- - sudden deterioration of the onboard camera picture,
- - the LOX valve failing to open,
- - kerosene seen dripping from the base of the rocket,
- - the internal fire
- - the explosion in the kerosene tank,
- - failure of the abort sequence to close the propellant
- valves, or disable the payload,
- - lack of concrete data with which to analysis the
- failure.
-
-
- A. Onboard Camera Picture Failure
-
- The sudden deterioration of the video picture took the form
- of saturated white horizontal bars forming about bright
- portions of the picture. During the launch, these bars were
- present to an extent, but not enough to really detract from
- the overall picture. However at the exact time the payload
- was switched to internal power, these bars suddenly swamped
- around 30% of the picture. Causing the telemetry personnel
- to call a hold.
-
- The horizontal bars were caused by solid state regulators in
- the actual camera shutting down (thermal limiting) after
- overheating. The camera had been connected directly to the
- rocket's unregulated power supply which is nominally 14V, a
- little higher than the camera's nominal operating voltage of
- 12V. The condition became drastically worse when the
- payload was switched to internal power because the lithium
- battery pack used to power the payload, was capable of
- supplying, initially, around 17V. The same effect was
- repeated in Melbourne, after fire damage to camera had been
- repaired. The camera was connect to a 14V power supply and
- allowed to operate for some time (around 20 minutes) until
- the horizontal white bars developed, then the power supply
- was raised to 16V, and a very similar effect was observed.
-
- The fault could have been avoided had the camera been
- connected to a regulated power source. In fact a 12V
- regulator was provided for the camera on the rocket's power
- supply, but this output had simply not been used.
-
-
- B. LOX Valve Failure
-
- The most obvious and vexing question of course, is the
- reason for the LOX valve failure. The original explanation,
- that a pneumatic line had burnt through at exactly the right
- moment seemed a little unlikely. At the last static firing,
- valve position sensors showed that the time taken for the
- LOX valve to opens is in the order of around 60ms [2], so
- for the LOX valve actuator to have moved 11% requires
- failure within a window milliseconds wide, an unlikely event
- indeed. Thus a reason which inherently moves the valve a
- small amount would be infinitely preferable to one which
- relies on split-second bad luck. Possible reasons
- investigated included;
-
- a) an electrical failure due to ;
- - an umbilical being disconnected,
- - an electronic failure in the Launch Sequence
- Controller (LSC) or it's power supply.
- b) a pneumatic failure due to;
- - a loss of pressure to the actuators due to a breach
- in the ON side pneumatics, a 1MPa regulator failure,
- or a pneumatic (Legris push fitting) fitting
- failure,
- - an electrical or physical failure in the pilot
- solenoid,
- - a failure in the vane actuator.
- c) mechanical failure due to;
- - the valve seizing due to mechanical distortion from
- cryogenic temperatures,
- - the ball freezing to the valve seat due to moisture
- being present,
- - the valve stem or perhaps valve sensors jammed due
- to ice build up,
-
- The majority of these possibilities were rejected simply
- because they did not satisfy the split-second timing
- problem.
-
- An electrical failure was discounted as the LSC's indicator
- lights showed that appropriate signals were being sent to
- the pilot solenoid valves. The LSC was tested later and
- proved to be fully functional.
-
- An ON side pneumatic line failure was seriously considered
- as a possibility. The kerosene leak in the lower valve
- fairing would have dribbled kerosene onto the pneumatic
- lines leading to the rocket. These lines would have ignited
- with the flare, severely weakening them. Conceivably then
- the kerosene plume exiting from the motor could have burnt
- through the lines then, as the timing was chosen such that
- the kerosene and LOX exit almost simultaneously. However
- high speed film shows no sign of the lines burning
- beforehand, and the kerosene plume does not exit the rocket
- motor for about 0.5s. It was also suggested that the
- kerosene leak may have lubricated one of numerous pneumatic
- couplings allowing a line to blow off. This was discounted
- by collecting all the push-fittings and checking that a
- piece of tubing was still firmly inside the fitting.
-
- A failure with the pilot solenoid was rejected mainly due to
- the timing reasons mentioned. Unfortunately, the solenoid
- was very badly damaged making it difficult to prove beyond
- doubt that it was operational.
-
- Originally the vane actuator was not even considered as a
- possible point of failure. However it was mounted directly
- onto the LOX ball valve, and its mechanism contains two
- seals which may not operate properly beyond around -20C. Had
- these seals failed, the expected response would match those
- observed very well. Thus a seal failure in the vane actuator
- is a preferable explanation, and is discussed in detail
- below.
-
- The actual LOX ball valve seizing from mechanical distortion
- was rejected out of hand as the valve is explicitly designed
- to handle cryogenic fluids. Freezing of the valve stem, or
- the position sensor was rejected due to the lack of humidity
- on the day. Even had a layer of ice formed, it is unlikely,
- given the small surface area, that it would have jammed the
- vane actuator. In light of the kerosene leak, it was
- suggested that the whole mechanism may have been frozen in a
- lump of kerosene ice. However if this was the case, than the
- valve would not have opened at all.
-
- At an earlier static firing (14/3/92) the LOX valve had also
- failed to open fully. Inspection of the valve afterwards
- showed that there was trichloroethane present in the LOX
- valve itself, a remanent from an earlier procedure to remove
- grease from the LOX feed system. This event caused the
- addition of a dry nitrogen purge to the launch sequence.
- Nitrogen is flushed through the LOX feed system, hopefully
- removing any residual solvents as well as any water vapour
- present in the tank. This procedure would appear to be
- successful as the following 3 static firings progressed with
- out a hitch. For this reason, as a dry nitrogen purge was
- performed, this theory was discarded.
-
- The vane actuator was used to actually turn the LOX ball
- valve. It was mounted directly to the body by an aluminium
- mount, and coupled to the valve stem via a slip on coupling.
- The aluminium block was machined to contact well with both
- the valve body, and the bottom of the vane actuator. This
- mount would have formed a reasonable thermal path from the
- body of the valve to the body of the vane actuator. The
- seals within the vane actuator are made from polyurethane
- and have a nominal working temperature range which extends
- as low as -20C. Beyond this temperature, the seals begin to
- lose their elasticity. LOX was present at the LOX ball valve
- for 40 minutes (30 minutes from the start of fuelling, plus
- another 10 minutes for the hold). With LOX having a
- temperature of around 90K, in the enclosed environment of
- the lower valve fairing, it is entirely possible that the
- vane actuators body temperature could have fallen to
- unacceptably low temperatures.
-
- If this was the case, then the vane would have "frozen" in
- the closed position. When the pneumatic pressure was
- applied, the vane would have hesitated and then moved
- possibly in "stutters". With the seal no longer plastic, the
- gas may also have burst under the seals delaying the
- movement even further. With the LOX valve partially open,
- the plume cuts through the pneumatic lines, while the vane
- actuator is still stuttering open, some seconds later. This
- would seem to be the most plausible reason for the LOX valve
- failure. Hopefully a test can be conducted utilising the
- Helium valve vane actuator (if it has survived) to confirm
- this. If this is the case, the abort may have contributed to
- the failure, as it added 10 minutes to the countdown,
- extending the time LOX was present at the valve by 33%.
-
-
- C. Kerosene Leak
-
- A leak in one of the kerosene valve's body connector seals
- was detected during final pressure tests the day before
- launch. As it was a gas leakage at a negligible rate, it was
- decided to ignore it. On the launch day, after kerosene
- fuelling, it was observed that no kerosene was leaking from
- the body connector seal. However after the LOX fuelling, and
- the sealing of the LOX bleed plug, it was discovered that
- kerosene was leaking from the bottom of the rocket [1].
-
- The leak in the seal itself was caused simply because the
- type of body connector seals used in the kerosene valve were
- in fact once-only seals, that is they deform to form a seal,
- but once the valve is disassembled they stay deformed, and
- should be discarded. This was not the case, the seals had
- been used four or five times already. The leak manifested
- itself only after the LOX tank had been sealed because of a
- design fault in the tank pressurising system.
-
- The LOX tank is self pressurising in the sense that the LOX
- is constantly boiling off, so that the pressure rises in the
- tank once it is sealed. The tank pressurising system was
- designed assuming that the tank regulators acted as check
- valves and thus would prevent backflow from a pressurised to
- tank back into the system [3]. This proved not to be the
- case. Once the LOX tank was filled, a small amount of oxygen
- under its own pressure flowed back through the pressurising
- system and into the kerosene tank. The amount of oxygen
- would have been very small, however this pressurisation of
- the kerosene tank was enough to cause the kerosene to leak.
-
- The kerosene leak in itself was probably not as major a
- problem as it sounds. However by dribbling down the
- umbilical, it supplied a path by which the exhaust plume
- could ignite the wiring loom inside the lower valve fairing.
-
-
- D. Fire Inside the Rocket
-
- A fire inside the lower valve fairing should not have been
- as major a problem as it was. A tiny volume, mostly sealed
- at the top, a fire should have quickly suffocated itself. In
- addition the insulation on the wiring loom was self-
- extinguishing, that is if lit by a open flame, the
- insulation does not continue to burn in air once the flame
- is removed.
-
- As was mentioned earlier, the LOX tank self pressurises. For
- this reason a relief valve is placed at the top of the LOX
- tank, and set to crack at 4.5MPa. The vent from this relief
- valve was not piped to the atmosphere, but left within the
- rocket. During the countdown, the LOX tank would have been
- slowly venting into the rocket body, and venting furiously
- during the 15 seconds after T=0s (as can be seen from the
- onboard camera). This would have provided a very oxygen rich
- atmosphere within the rocket, allowing the looms to burn up
- the rocket as far as the payload, eventually destroying it.
- The amounts of oxygen present can be seen from the severe
- "weathering" of all the aluminium parts after the fire.
-
-
- E. Kerosene Tank Explosion
-
- As mentioned earlier, oxygen was able to bleed back, through
- the LOX regulator, from the LOX tank to the kerosene tank.
- After all the kerosene had been expelled, and the helium
- pressurising gas vented, oxygen bled back through the
- pressurising system to forming a fuel air mixture within
- the kerosene tank. When the mixture ratio was right, it
- ignited from the small kerosene fire seen at the at the base
- of the motor. The flame travelled back through the motor's
- cooling passages, and through the injector into the kerosene
- tank. The residual kerosene may even have been burning
- inside the kerosene tank for a while before exploding.
-
- The explosion ruptured the LOX pipe conduit, at its weld to
- the top of the kerosene tank boss. The hot gasses then
- expanding down through the LOX pipe conduit into the lower
- valve fairing. The lower valve fairing hatch's backing plate
- was buckled and then blown from the rocket, coming to rest
- on the launch apron ring road. The upper valve fairing hatch
- was likewise torn out. Some gas rushed upwards through the
- pressure line & wiring conduit into the electronics fairing,
- breaching the camera's case and pushing the main parachute
- out of it's tube. The bolts holding the intertank to the
- bottom of the LOX tank boss then sheared, breaking the
- rocket it two. The upper launch lug broke, and the rocket
- was thrown to one side. The LOX feed line ripped from it's
- fitting at the base of the LOX tank, and the thrust produced
- by the LOX being expelled was sufficient to lift the top
- half of the rocket, through the air and then along the
- ground for some distance. The bottom half of the rocket was
- also torn from the launcher, and fell to the ground nearby,
- the remaining kerosene visibly burning for a several
- seconds.
-
- The bleed back through the regulator was more complicated
- than just simple two-way flow through the regulator. It can
- be shown that had the LOX valve completely failed to open,
- then the events leading to the explosion could have been
- avoided (see Appendix A).
-
-
- F. Abort Sequence
-
- Originally the rocket was designed with no abort system at
- all, however at the static firings it was discovered that
- the existing pneumatics could, with the addition of a few
- lines, allow the propellant valves to be closed as well as
- opened. This system used at each of the static firings, and
- then incorporated into the rocket itself, if only as a
- convenient method of shutting the valves during tests.
-
- The abort system was actuated at about T+2s, but was unable
- to close the propellant valves because the pneumatic line
- used to close the valves had already burnt through in the
- exhaust plume of the rocket. Likewise the payload could not
- be disabled because the electrical umbilicals also burnt
- through. The failure of the abort system is the most
- unacceptable of all the failures as it was thoroughly
- predictable, and easily avoidable.
-
-
- G. Lack of Data
-
- Most of the analysis involved a large degree of speculation
- because little data of the failure was available. All of the
- cameras were placed to take rather optimistic "long" shots.
- So no clear picture of the base of the rocket is available.
- This was compounded with problems with the payload which
- resulted in critical data such as the tank pressures, and
- the valve position sensors being lost.
-
-
-
- III. SOLUTIONS
- ~~~~~~~~~~~~~~~
- "For every problem there is one solution which is
- simple, neat, and wrong."
- H. L. Mencken
-
- With "20/20: hindsight, it is easy to propose simple
- solutions to many of the problems which have already
- occurred. The real solution is to actively try and find all
- the possible failures have not occurred and to either
- prevent them or at least have procedures as to what action
- to take, when they occurred. As a case in point, the payload
- could have been disabled in the first 20 seconds after the
- failure, as the electrical lines where still intact.
- Although this would not have saved the rocket, at least it
- would have prevented some media embarrassment.
-
- The abort system and payload umbilicals should have been
- heavily protected from the exhaust plume. An E-flux
- deflector could be welded to the base of the launcher. The
- pneumatic lines running to the rocket, as well as those
- inside should be replaced by stainless or aluminium tubing.
- The 1MPa pneumatic supply should be moved much further away
- from launcher, and protected. The electric umbilicals could
- be connected high up on the rocket so as to be out of harms
- way. The close valve could be placed inside the rocket so
- that there is only one pneumatic line leading to the ground.
-
- Check valves should be installed after the each propellant
- tank regulator in order to prevent the bleed back of gases.
- Both the LOX and kerosene relief valves should be
- repositioned so that they vent to the atmosphere, not the
- inside of the rocket.
-
- All components used should be carefully studied so that
- items such as non-reusable seals are replaced, and normal
- operating conditions are not exceeded. The current LOX valve
- arrangement could be used with the addition of a thermal
- insulator such as a plastic or ceramic plate between the
- body of the vane actuator, and the valve body mount.
- Extensive testing of each of the possible valve failures
- should be investigated under realistic conditions (using
- liquid nitrogen) and worst case data should be obtained.
-
- An automatic abort sequence could be added to the LSC in
- order to cut down response time assuming appropriate
- telemetry data is available. Better displays of realtime
- engineering data would also allow better decision making.
- Finally, more formal procedures, especially launch/abort
- criterion need to be established beforehand so that these
- decisions are not made "in the heat of the moment".
-
-
-
- IV. CONCLUSION
- ~~~~~~~~~~~~~~~
- "You may be disappointed if you fail, but you are
- doomed if you don't try."
- Beverley Sills
-
- AUSROC II failed to lift off because the LOX valve failed to
- open fully. The most likely explanation is that the valve
- only partially opened because the seal inside the LOX
- valve's vane actuator failed due to prolonged exposure to
- low temperatures. The sudden deterioration in the live video
- signal was due to incorrect wiring of the video camera's
- power supply. The 10 minute hold caused be the camera
- problem may have contributed to the LOX valve failure. After
- the LOX valve had failed to open, it should have been
- possible to save AUSROC II by closing the propellant valves,
- and disabling the payload. This was not done, as the wires
- and pneumatic lines associated with the abort system, were
- not protected in any way, and therefore burnt through in a
- matter of seconds. Simply shielding the wires and using
- stainless steel pneumatic lines would have avoided this
- problem. An automatic abort sequence based on telemetry data
- would allow the launch to be aborted the instant a valve
- failure is detected.
-
- The explosion which destroyed the vehicle was caused by
- oxygen flowing backwards under its own pressure, through the
- LOX regulator into the kerosene tank. Residual kerosene
- vapour in the kerosene tank mixed with the oxygen to form an
- explosive mixture. The backflow occurred due to a design
- fault in the pressurising system, a check valve placed
- before or after the LOX regulator would prevent the problem.
-
- The kerosene leak was caused by a non-reusable seal being
- reused in the kerosene ball valve. This leak provided an
- ignition source for the fire inside the rocket, and while it
- contributed to the destruction of the payload, it probably
- did not contribute otherwise to the launch failure. Although
- the wiring looms were self-extinguishing, the placement of
- the LOX relief valve vent inside the upper valve fairing
- provided an oxygen rich atmosphere within which they could
- burn. The relief valve should be placed so that it vents
- directly to the atmosphere.
-
- If AUSROC Projects is to continue another AUSROC II
- (designated AUSROC II-2) vehicle needs to be built. An
- opportunity now exists to incorporate all of the changes
- which had been suggested during the construction of AUSROC
- II-1, as well as the changes suggested here.
-
- The design of AUSROC II was in many ways too "positive".
- Much thought had been put into each of the systems, but
- little thought had been allocated to possible failures and
- their consequences. Obviously, greater testing of each
- component may have shown up some of these problems earlier.
- This simply highlights the very limited resources with which
- the group currently works. The six static firings were in
- themselves, major system tests, but they were already a
- major strain on our resources. Hopefully AUSROC II-2 will be
- able to proceed in an environment where financial and man-
- hour constraints become secondary to the process of
- engineering.
-
-
- References
-
- [1]AUSROC Projects, AUSROC II Launch Campaign Review, 26
- October 1992
- [2]A. Cheers, Static Firing Data - 25/4/92 1st Firing, April
- 1992
- [3]M. Blair and P. Kantzos, Design of a Bi-Propellant Liquid
- Fuelled Rocket, Final Year Project Thesis, Dept.
- Mechanical Engineering, Monash University, 1989
-
-
- Author
-
- Tzu-Pei Chen Phone: (03) 561 8654, 560 8629ah
- Ardebil Pty Ltd FAX: (03) 560 5562
- 6 Kooringa Crescent Pager: (03) 483 4206
- Mulgrave VIC 3170 Email: chen@decus.com.au
-
-
- Previous AUSROC updates can be obtained by anonymous ftp to
- audrey.levels.unisa.edu.au in directory space/AUSROC
-
- --
- Steven S. Pietrobon, Australian Space Centre for Signal Processing
- Signal Processing Research Institute, University of South Australia
- The Levels, SA 5095, Australia. steven@sal.levels.unisa.edu.au
-